2014/08/02 17:08:18
MR PLOW
Not too long now - W2A heat exchanger is in, harmonic balancer should arrive Tuesday, the guys can put the head back on and engine in. Then ECU time, tuning and give it a whirl. Can't wait!
Degreased the engine bay today (forgot pics sorry) - I think I've saved 1-2 kgs of weight with that gunk gone!
  
2014/08/02 23:22:24
B24
Nice work, looks like you are ticking all the right boxes.
2014/10/31 21:13:37
MR PLOW
So here's the latest. I picked the car up last weekend, which was fantastic after almost 6 months! Scrubbed up well with a wash, and feels so good to drive! Dyno showed 280 hp (209 kw) at a debatable boost level - ECU and guauge were showing 16psi, the dyno showing about 18. Anyway, a solid improvement over the previous 185 kw at 15ish and leaning out! Still a bit bumpy there on the AFRs...
Work done includes...

Engine rebuild: Bored & honed, crankshaft grind & balanced, Block decked, O'haul Oil pump, head serviced, head & manifold ported, new water pump, thermostat, plugs. Parts inc CP forged pistons (.020" oversized), Eagle Rods, Cometic metal HG, ARP head studs, ARP main studs, ACL bearings main, rods& thrust(main & rods 0.010"), Full OEM gasket & timing kits, OEM crank pulley (harmonic balancer), Fidanza Lightweight flywheel.
Fueling & IC upgrade: Frozenboost W2A IC (type 3) and front mount heat exch (type 100 = 24x12x1 inch), cheapo Rule water pump, Walbro 255 Lph fuel pump, Wolfkatz Top Feed Fuel Rail, Bosch(ID) 900 cc/min High Imp. Inj. + Clips. 
ECU: EMS EM70 & MSD Ignition unit
AirCon deleted, 4pt harness installed.
 
Took it to Wakefield on Wednesday, and almost cried on the way down - 4 gear pulls produced much earlier boost than before, but quickly changed into the flutter I now know as compressor surge! The day wasn't wasted, but I could only power up gradually out of corners, and recorded fairly limp 1:17's (there's some serious driver improvement potential here also to be honest :-). Acceleration down the main straight was great though, matching most of the cars there and it sounded good! The compressor surge probably wouldn't be an issue if I took more corners in 2nd but it's very offputting. So hopefully can sort that with some tuning tweaks or else turbo/cam work (or other suggestions?)
The W2A was flawless, after each session I felt the intercooler and it was cold, so really pleased with that. Should be able to get some logs off the tuner in a couple of weeks to see how the intake temps etc went. 
2014/11/12 07:24:58
MR PLOW
Tuner has dialled the boost down just enough at low-mid rev rates to knock out the compressor surge, feels much nicer now to have the confidence to plant it!
(Edit- famous last words, still a problem, and now post- Christmas there's oil in the intake...)
2015/01/08 17:43:59
MR2QIK
Think I just saw you near Homebase Prospect earlier today. Looks good. I was in the MR2 & briefly caught you @ the roundabout before going in the opposite direction.
2015/01/08 18:35:35
MR PLOW
Lol, was there smoke coming out of the exhaust? Might be my car, it's with Paul Brell at Girraween to try and sort my turbo oil leak/ compressor surge ahead of the MTC, so right neighbourhood. Plate MI57ER?
2015/01/08 21:01:24
Admin
Your setup is similar to mine. Has your turbo been high flowed? 16psi is the most I can run due to intake temps being too high above that level. I'm at the limit of what the turbo can pump. Mine leaks oil a little bit too. My old ST185 GT4 did too. It seems to be a common problem with the ct26


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2015/01/08 22:06:28
MR2QIK
Was your car I'm certain. Wasn't directly behind it for more than a few seconds. I saw him rev it out a bit in the opposite direction & didn't notice any excessive smoke.

Btw, the stock ct26 is really useless past 16psi anyway. I know this one is "high flowed" though so shouldn't apply.
2015/01/08 22:58:40
Admin
I haven't seen anything above 210kW with a high flowed ct26 though you can get up to 250 with e85 due to reduced temperatures




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2015/01/08 23:00:28
Admin
I got 250 on my old 2L engine with e85 and 23psi

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