Was great to spend a few hours at Wakefield on Sunday. Was also excellent to have Ian and Pete there for a drive and meet up for a chat. Just looking forward to the day when we can have a drive, chat, then drive again without all the manic work to get the car sorted for the next session. Was also great to meet up with Adam with his newly aquired SW20 Tarmac Rally car. Very nice and quick piece of kit which I hope to see again in the new year.
The car is still having teething issues but it was great to run the car and find the problems before the trackday in Jan. Turns out the coil was more than likely a bad wire which was fixed yesterday only to find out three of the four turbo mounting nuts had fallen off! No wonder the engine bay was a little hot..The manifold wil be removed over the next few days then wrapped in hitemp titanium wrap with a sock fitted to the exhaust housing, the coolant pipe will also be wrapped, the orginal rear windscreen will be replaced as the lexan unit was damaged due to heat, turbo housing studs will be welded to the exhaust manifold with interferance nuts fitted.
The brake pedal feels very long but it may simply be lack of brake pad as I could still lock the wheels up under braking but still effected confidence in late braking. Still havent sorted the balance just yet but its getting there. If you hold it flat through the kink then brake hard then turn in when you run out of track to pull it up, it will still step out which entering the apex. Great for setting up for drift/powersliding but would be better if it would be a little more settled with less slip angle on entry to the corner.
Electric water pump was working perfectly. Set it at 85 and it never moved.
Oil never moved passed 90 at any stage but its still not being run at full potential so will have to see if it can manage it when it is sorted.
Exhaust temp was 650 but I think the other 200 was being released into the engine bay when the bolts came out.

Water injection was also working fine. You can hear it working very clearly but Im having trouble with the data logger so I dont know how much its helping intake temps under load.
At least the alternator is working fine relocated to its OEM location. Funny that..
Im not all that happy with the tyres. They were suspect at Winton and when I was pushing a little in the second session on sunday, the same thing happened. When pushed, they get hot then fall off over then require management which slows you down.
If I can manage a 1.08 with these tyres when its running at the 330rwhp as it was tuned, I will be pretty happy.