I have now taken 50Kg out of the car! That should make a noticeable difference to my lap times.
I have a dyno session booked for Tuesday to make sure everything is OK and to also see if I can run some additional boost seeing how I now have a better intercooler pump. I'm hoping that the improved intercooling will give me some more power.
I'm also hoping that the inlet valves working properly will make the engine work better too.
It now starts, idles and free revs perfectly. Those of you will remember the car at the last MR2TC coughing and farting a lot due to the ****ty Ferrea inlet valves. The only thing I have changed in the engine is the inlet valves. Everything else is the same as at MR2TC 2014 so the valves were definitely the cause of my issues then.
FYI Ferrea are still refusing to admit that their product was faulty. F them!